Stretch or ppsi torque I think either will work as I hope you have a rev limiter installed or it might just do the same thing again. Blowers stress all engines, no matter who builds them. JMHO-----which aint much these days.
Thanks T.... My new torque wrench has a certificate showing tests done at different poundage's. It tested dead on up to 200lbs and showed 249.8 lbs
at a 250lb pull. I am going to do as Rick said and torque the bolts several times to wear them in before final torque at 70lbs. I will check for stretch
and add more torque (if needed) to even out the stretch on all bolts.
I have been going over the failure so much to pin point what went wrong, and have come to the conclusion that it was a number of things that compiled into it. #1 reason I feel is that I must have over stretched the bolts. I say this because I can remember hitting the torque spec needed, and it
just did not feel that it was enough. I can remember giving it just a bit more after the click on the two rods that broke. I remember this because it was those two rods that I had to remove the caps after I had them all on, because I had forgot to mic and record the crank journal. Looking back...When I reinstalled those caps ... I feel that there was a chance that they may have not been seated down all the way, and may have bound up on the dowels.
I just remember them feeling spongy.. # 2 If you go back and listen carefully to the video link I posted... at the end of the video where I came down off the motor and walked around the passenger side of the truck , You can hear me make a remark about how I thought I heard some noise in the pan.
If you listen carefully... you can hear ( which had to have been the rods) hitting the windage tray. That could not have been good on those bolt heads.
Also the tune I had was questionable, as I am learning about this Super Sniper EFI. It may have caused some detonation. Then there is the fact that I DO NOT have a rev limiter, and I may have over revved it on the test hit. I have always relied on my shift light to do my shifting. On that first test hit... My tach was not hooked up yet, and I was relying on watching that hand held monitor for my RPM's.. and feel.
Everything and senario I have gone over...I have come to a conclusion with.... it all points to ME. I was so excited about trying to meet a deadline for the next event... I lost focus and did not question myself enough, when subtle little things (like spongy feel on the torque) arose and I just pushed forward.
It was a recipe for disaster.
I am taking my time with the new build. Not to say I did not with the first one, but I will be questioning alot more of myself.
After the motor is back together, I have already talked to "Steve Morris Engines" and he is going to dyno and tune the motor before I put it back in the truck. I will feel alot better having someone with his expertise going over the motor and putting the correct tune on it. Especially with the E-85 fuel and that Sniper EFI.
My wife meanwhile said that at the very least....from all of what has happened.. she has finally found what it takes to make me humble....... A broken motor to the tune of $12,000
Also T..... dont ever short change yourself or your opinion... It does count!