Sorry for the delay Men...I fell ill for a few days.
Ok..Yesterday I felt better enough to head for the barn. Coty stopped by to lend a hand. After connecting the white wire, we did get spark!
Only it was 180 degrees out..
After removing the valve covers and verifying the valves were lashed correctly , ( took no chances on anything) we reinstalled the distributor
180 degrees.
Not bad so far...
After all checks were made... we hit the start button only to hear metal hitting metal sound!!!!!
We removed the valve covers again to see if I missed anything... ALL was GOOD.
So we removed the blower belt and rotated the rotors to see if maybe something had fell in. Again all checked good.
At this point we just sat back and replayed the build and went over documents I had made.
We pulled all the plugs and turned the motor over by hand . There was
NO bind or interference to be found!!!!!
After one more cup of coffee I seen that the teeth on the flex plate Had metal removed from them. Then I seen some shavings on the floor
under the stand and flexplate.
We found the culpurate! After removing the starter....Coty chucked up on each bolt with a battery drill and found that the bolts were bent pretty bad. We made a trip to the parts store for new starter bolts and decided to have the mini torque starter replaced as well (it had a lifetime warrenty).
With new bolts and starter installed...and giving the motor another look over, we decided we would try to roll the motor over with no plugs
or spark..
It was quiet!!!!!
We installed the plugs and connected the fuel pump and the coil wire...also said a prayer !!!
The E-70 fuel we were using for a test start was not wanting to lite in the cold temperature, but it soon did!
We checked the oil pressure (50 lbs).
Listened for any out of ordinary sound and found nothing.
We found that the idle A/F was at 8.2 which is very rich. Should have been near 10 with E70.
But we were not tuning....We were looking for a solid smooth running motor.
After the video... we hooked up a timing light and found that the motor was hunting for an idle. We set the static timing at 15 degrees according to Holley. Timing was bouncing a few degrees around the 15 degree mark because of the hunting issue.
This will be close enough for Steve to dial in when we run the VP- C85 in a warmer enviroment.
There were no leaks around the pan where I had fixed it, or anywhere else.
There was no knocking sounds anywhere !!!!!!!
We decided to shut the motor down after bringing it up to operating temp and call it a successful rebuild (so far).
We are putting the engine back on it's cradle and bolting it to a pallet that we will box in with plywood for the trip accross state to see Steve on the 17th.
Enjoy the video!